Final Flight of the Ghost

Автокөліктер мен көлік құралдары

This is a video of Jimmy Leeward's final race. This video shows no impact with the ground just the events leading up to the accident, segments of this footage have been turned over to the NTSB to help with the investigation.

Пікірлер: 743

  • @kellybrowning7117
    @kellybrowning711710 ай бұрын

    Just took the time to watch this and it brought back alot of bittersweet memories. My family and I were sitting just a few rows behind the point of impact that day, and in retrospect, it was definately one of the hardest things I've ever had to witness. I'd never met Jimmy, but I'll forever be a fan of his legacy and the roll he played in shaping the sport of air racing. We used to travel to Reno for the air races every couple years, prior to the crash, but haven't been back since. This year is different. Being the last year it will ever be held in Reno, I couldn't let it pass without a proper goodbye, so off we go. Thanks to all the great pilots (looking at you Jimmy) and teams for a great run. It's been my honor to cheer you on for all these years.

  • @FrankKingstonSmith
    @FrankKingstonSmith12 жыл бұрын

    I was the lead announcer for the races at Reno... have been since 2002. Steve Stavrakakis, also a fine airshow pilot, is my co-announcer and color guy for the unlimiteds. The sad event is etched into my mind for keeps. As was the incredible rescue effort which followed. A real tough afternoon.

  • @davecrupel2817

    @davecrupel2817

    3 жыл бұрын

    Checking in 9 years after you left this comment. Are you still the lead announcer at Reno? (Not counting covid times) And do you know if Reno will continue post-covid?

  • @FrankKingstonSmith

    @FrankKingstonSmith

    3 жыл бұрын

    @@davecrupel2817 I announced one more year. Every time the heavy iron came around the pylons to our left, I ducked. I couldn't get the image of the "Ghost" coming at me the year before. Actually, I left the industry after that.

  • @bigmandan4090

    @bigmandan4090

    3 жыл бұрын

    @@FrankKingstonSmith I’m real sorry to hear that man, I hope you’ve found peace now, that day was tragic.

  • @Arafat.Abou-Chaker

    @Arafat.Abou-Chaker

    2 жыл бұрын

    @@FrankKingstonSmith so you are the guy who can be heard in the footage? You did an amazing job at keeping the audience from panicking!

  • @jaegertiger384

    @jaegertiger384

    Жыл бұрын

    @@Arafat.Abou-Chaker May God bless him for his professionalism and commitment to the honor of a great pilot.

  • @tcwhite0104
    @tcwhite01048 жыл бұрын

    total irresponsibility on Jimmy and the crew!! You NEVER take shortcuts on aviation equipment of any part...document, document and document!! every thing...RIP Jimmy...

  • @johne1031
    @johne10319 жыл бұрын

    As an old and somewhat bold pilot told me back in the day -- flying is not inherently dangerous, but it is absolutely unforgiving.

  • @Jonno2summit

    @Jonno2summit

    9 жыл бұрын

    Well said.

  • @ArchTeryx00

    @ArchTeryx00

    9 жыл бұрын

    John E It also heavily depends on the *type* of flying you're doing. Losing an elevator trim tab when you're flying a Cessna 172 in cruise is an easily recoverable event. Losing that same trim tab in a race plane, at racing speeds, instantly results in an uncontrollable aircraft. As we sadly found out.

  • @huey9080

    @huey9080

    7 жыл бұрын

    John E UND DAS

  • @stihlnz

    @stihlnz

    7 жыл бұрын

    The original quote "Aviation in itself is not inherently dangerous. But to an even greater degree than the sea, it is terribly unforgiving of any carelessness, incapacity or neglect." - Captain A. G. Lamplugh, British Aviation Insurance Group, London. c. early 1930's.

  • @gukakmakuk

    @gukakmakuk

    7 жыл бұрын

    It kakes special aviation wisdom to never flirt with real danger

  • @clutchcrgo
    @clutchcrgo12 жыл бұрын

    This is the absolute best air racing tape that I have ever seen, and I have looked at a few. The engine starts, the sounds of the engines running @ takeoff power: you captured it all, not to mention the exact instant at which the late Jimmy Leeward's Galloping Ghost departed controlled flight, never to return. You have a gift, Voodoo 1650, God bless you. I am sure that you have helped the NTSB immensely with their investigation. Clutch

  • @gunnersdoubleott
    @gunnersdoubleott11 жыл бұрын

    Great respectfull video. Thank you! Unfortunately I was there and lost some family Friends as well. Forever etched in my mind. Fortunately Reno lives on.

  • @davecrupel2817

    @davecrupel2817

    4 жыл бұрын

    I'm so sorry about your family :( R.I.P. I hope you can still enjoy aviation after that...

  • @elementxxrider

    @elementxxrider

    4 жыл бұрын

    May they rest in peace bro. Heartfelt condolences

  • @cujet
    @cujet12 жыл бұрын

    Thanks so much for producing this and sharing it. I met Jimmy at a hangar party a few years back. One of the very best guys!

  • @JB-zn1kx
    @JB-zn1kx Жыл бұрын

    11 years ago... I was sitting in those stands. I'll Never forget the sound

  • @Channel58
    @Channel5812 жыл бұрын

    Great Video, thanks for sharing. This has to be one of the best short videos showing the Reno air race. Great start up and view of all the competitors. Too bad it has to be connected to such a great tragedy. You can tell the videographer has a great love of WWII planes like most of us. Great job!

  • @Sumtoshi
    @Sumtoshi9 жыл бұрын

    I was here when this happened. I was sitting right where the plane went in and all of my neighboring spectators were killed. For some reason got out of my seat 3:45 before the crash and filmed the race, and jimmies rapid climb/fall into seats. Very emotional day and I became close with the FAA folks there afterward. Hope you can keep what's important in focus in this forum.

  • @ralphj.cuevas6523

    @ralphj.cuevas6523

    8 жыл бұрын

    Air Show Spectators: My condolences, Also go to the Families and Friends of the spectators watching the show.

  • @Astinsan

    @Astinsan

    5 жыл бұрын

    Sorry you had to be part of it. I don’t agree with the faa and NTSB findings Though. I do place the majority of the blame on the company putting on the race. All of the planes were modified. On a auto race track you have to pass technical (or be teched ) it appears there wasn’t a real technician on site with proper agreed upon specifications for each aircraft with an FAA sign off. Since this race has been going on since the 60’s the FAA was on notice so the other part of the blame should be on them. I don’t fault to pilot at all as he was forthcoming prior to death about modifications done to the aircraft. This is what happens if you are complacent. Peoples lives are at risk. It’s extremely sad. You can see the pilot tried regain control when that rear elevator broke off. Really horrific scene.

  • @Dartman6

    @Dartman6

    4 жыл бұрын

    Pilot Jimmy Leeward was knocked unconscious at the time of upset and 17G load. It was impossible for him to "try to regain control" when the elevator trim tab broke off.

  • @DoctorShocktor

    @DoctorShocktor

    4 жыл бұрын

    Jason Brooks Yeah. Your opinion is meaningless and your conclusions are wrong. Thank God we’ve got professionals to evaluate these situations. You are laughably mistaken on every point.

  • @utube321piotr

    @utube321piotr

    4 жыл бұрын

    @@Astinsan the pilot in this tragedy was more focused on speed than on the common sense safety to say the least; you seem to think as if the owner/pilot was unaware of the ultra high performance character of his aircraft and put blame on organizers; he cut all 4 wings to gain speed, put lots of money and effort yet failed to address the rudimentary basics

  • @AReallyBuffLlama
    @AReallyBuffLlama11 жыл бұрын

    Absolutely gorgeous. Me and my dad went down to the valley of speed at Reno in 2010, and watched Ghost in action. She was such a beautiful plane.

  • @themomentchannel3498

    @themomentchannel3498

    Жыл бұрын

    and a flying time bomb, it was a matter of time before the elevator trim tab failed since the plane used old counterfeit parts and was not properly maintained.

  • @BeselerSimRacing
    @BeselerSimRacing8 жыл бұрын

    His age had nothing to do with the incident as well as the overall age of the aircraft. As far as not telling the FAA about modifications the only modification he notified them off was the boil off cooling system to which the FAA recommended 3 hours of flight testing to which were never completed. As far as the trim tab, they were using were self locking fiber nuts which are to only to be only used one time. Upon examination the NTSB found yellow paint underneath the top layer of paint on the lock nut. The aircraft at one point had been painted yellow but that was around 20+ years prior. In fact, the crew of galloping ghost even told the NTSB that they had to tighten the lock nuts on the ghost prior to going to Reno, evidence that this was a problem before they even got there. Yes, when you go to a race whether air racing or auto, you assume a risk. But is it out of line to assume that the competitors and the governing body of those machines have done everything they can to ensure that proper maintenance has been achieved? To me it's not out of line. This absolutely could have been avoided had the right technical oversight and practices been put into place before Race 177 even was permitted to take off that Sunday. Personally in my opinion this is negligence to the tenth degree. Never mind that the fuselage was wrinkling and their was a sizable gap between the windscreen a canopy as Leeward pushed the aircraft faster than it had ever went. If you take off in a Cessna 172 with full fuel and a full passenger load of 3 other dudes who weigh 220 pounds a piece and you snap the wings off would you still just say, "well aviation is dangerous!" Everyone here playing armchair A&P or NTSB investigators need to stfu. Read or watch the NTSB report. The people that investigated this incident have more degrees and more knowledge in engineering than 99.9 percent of you. Shit, even Avweb's Paul Bertorelli said the NTSB got it right. www.avweb.com/blogs/insider/AVwebInsider_GallopingGhost_207267-1.html Personally I can't help but get extremely pissed off when I see people stick up for that team. Jimmy Leeward was a fucking cowboy and the amount of negligence that went on is disturbing. Take the time and watch or read the official report here: kzread.info/dash/bejne/d4GhyrGkiLSoYNY.html www.ntsb.gov/investigations/AccidentReports/Pages/AAB1201.aspx

  • @casey19660

    @casey19660

    5 жыл бұрын

    Fact is who gives a shit what you think fucknut.

  • @alancoles3373

    @alancoles3373

    5 жыл бұрын

    @@casey19660- à

  • @alancoles3373

    @alancoles3373

    5 жыл бұрын

    @@casey19660

  • @ErikJohnston
    @ErikJohnston12 жыл бұрын

    Awesome video Jason. Thanks for letting me use your footage for our tribute video Im working on. Can't wait to meet you sometime.

  • @19sloper
    @19sloper12 жыл бұрын

    Voodoo, my compliments on an excellent video. And my appreciation for you sharing it. You did a fine job of camerawork, editing, and presentation with feeling. The Ghost was so beautiful, sleek, and sexy, even in its plain paint. I loved the concept and the approach Jimmy came up with to go fast. The challenge he threw down to his friends at Strega would have been an adventure to watch. It is all very sad, and somehow inspiring at the same time. I'll be back next year.

  • @Bushwhacker-mb3uh
    @Bushwhacker-mb3uh3 жыл бұрын

    Shame on all of you here singing this old man’s praises. Regardless of what kind of gentleman he may have been in life, he was selfish, negligent, and borderline criminal in the manner he modified his plane and concealed the modifications to avoid accountability. He was no hero. He was pulling 17+ G’s and was out like a light before that plane became a missile that stole 10 lives that day. He took advantage of the trust of the racing governing body, his peers, and tragically the fans that he killed attempting to gain an advantage in this race. He cheated the race but didn’t cheat the grave consequences for his irresponsible actions. It’s a shame 10 innocent people had to go with him. He was unconscious before that plane hit the crowd closest to the runway. He was no hero and he didn’t save any lives by making any alleged adjustments to avoid the stands and killing even more people. He was out like a light when he hit that crowd.

  • @FiveCentsPlease

    @FiveCentsPlease

    3 жыл бұрын

    +Daniel Maddox The plane was assembled by a team of people, so there was decision made during the construction process to use the old flight control parts which failed--and that choice could have been made by one or multiple people. It may be that the pilot was a casualty of that decision process. Ultimately, more flight testing should have been performed before race day and there is a lot of blame to share for that too, including the pilot/owner.

  • @kiwicory100
    @kiwicory10010 ай бұрын

    I’ve been to a lot of air shows and air races over the years and have personally been close to many a mishap and had met many of the pilots, performers, and ground crew. This tribute was a fitting testament to the golden days of the Reno Air Races. I don’t know what comes next for the races as a whole, but blessings and prayers to a truly sterling group of aviation enthusiasts! ❤❤❤

  • @privatepilot4064
    @privatepilot4064 Жыл бұрын

    You can actually see the trim tab separating during the climb. Legendary machines flown by legendary pilots.

  • @sanfranciscobay
    @sanfranciscobay10 жыл бұрын

    Is the canopy on Strega and Voodoo and the way it moves backward and forward identical, or do they just look similar in design from a distance?

  • @phlodel
    @phlodel10 жыл бұрын

    When fitted with the Merlin engine, the P 51 developed a problem with overload of the tail at speeds in excess of 500 mph. Although it was known that the fuselage needed to be extended to cure this problem, the P 51D did not get this modification due to wartime demands. This problem was not addressed until the H model. This inherent problem did not cause a problem in level flight with the stock aircraft. I've got to believe that this had something to do with this accident.

  • @johnbuffaloe9160
    @johnbuffaloe916010 жыл бұрын

    Beautifully done. Thank you.

  • @195511SM
    @195511SM12 жыл бұрын

    I was out there the day before ( the only day the Thunderbirds were scheduled to perform...) and had planned to return on Sunday for the finals. Condolances to Jimmy Leeward, his extended air racing Family & all of the fans. May the Reno Air Racing tradition live on. I can't wait!

  • @MarceloSabat
    @MarceloSabat12 жыл бұрын

    whos that song at the end of the video? thanks!

  • @BE36pilot
    @BE36pilot12 жыл бұрын

    With the initial pull-up(11G) exceeding the tail wheel down lock limits of 8.5G followed by an over 25G pitch the failure of seat or aft tank attachments used for coolant would be logical. I understand that in cockpit video shows Jimmy unconscious slumped down in the corner of the cockpit. The current thinking is that the root cause CG related not the trim tab failure. Jimmy was very experienced long time race pilot & QB, everyone I talked to thought very highly of him. RIP Jimmy

  • @joelallen9040
    @joelallen90402 жыл бұрын

    Thank you for the wonderful tribute, and not showing the crash and aftermath. Was very close to the crash site and the scenes still bother me.

  • @johncrazycat
    @johncrazycat12 жыл бұрын

    this is the best video footage that i have seen before the crash. RIP Jimmy and all those who passed. certainly the trim tab was to blame after watching this peice. thanks

  • @jimstand

    @jimstand

    2 жыл бұрын

    No, jimmy was to blame for not maintaining his plane.

  • @HHacker1959
    @HHacker195911 жыл бұрын

    We lost a good friend that day. Could you tell me the name of the song that was played in the end? It was so fitting for the tribute!

  • @natejohnston480
    @natejohnston4806 жыл бұрын

    I feel bad for the guy in the beginning cheering for Jimmy... RIP Jimmy

  • @MachTucker737
    @MachTucker73711 жыл бұрын

    by any chance do you know if the 'original' is a normal 'piston aircraft? I've seen some recently and they were turbine. This is one of my favorites. I should know more about it.

  • @FlightVideoPhoto
    @FlightVideoPhoto12 жыл бұрын

    Hi, thanks for sharing this beautiful video!

  • @joeysplats3209
    @joeysplats32095 жыл бұрын

    Thanks for keepin' it real, Voodoo.

  • @brucemckelvy9920
    @brucemckelvy99203 жыл бұрын

    I was there that day and will never forget it. Was on a motorcycle trip to all the lower 48 states and came the Catholic Church just outside the airport.

  • @bonnydonny
    @bonnydonny12 жыл бұрын

    @BE36pilot I wonder if the aft tank or pilot seat attachment failed? This video shows the tail wheel extending rapidly at the moment of loss of control, and we know Jimmy's head was not visible in many photos, possibly also this video right after loss of control. Sudden change of CG when the internal structure somehow failed, suddenly dumping the pilot down out of sight?

  • @Hallands.
    @Hallands.5 жыл бұрын

    The NTSB investigation report, released in August 2012, found that the *probable cause of the crash were reused single-use locknuts* in the left elevator trim tab system that loosened. This led to a fatigue crack in an attachment screw and allowed the trim tab to flutter. This flutter caused the trim tab link assembly to fail which led to loss of control of the aircraft. Untested and undocumented modifications to the airplane contributed to the accident. Particularly, the right trim tab had been fixed in place. Had both trim tabs been operational, the loss of the left trim tab alone may not have caused loss of control.

  • @FiveCentsPlease

    @FiveCentsPlease

    5 жыл бұрын

    +Hallands Menved Correct on all comments. Gotta wonder if the starbord trim tab had been operational, recovery may have been possible.

  • @Hallands.

    @Hallands.

    5 жыл бұрын

    FiveCentsPlease NTSB said "perhaps it would have been" and tightened the maintenance controls on show planes...

  • @FiveCentsPlease

    @FiveCentsPlease

    5 жыл бұрын

    @@Hallands. The FAA also told all Mustang owners that they are no longer compliant until those lock nuts and trim parts were replaced immediately.

  • @deanwoolston4794

    @deanwoolston4794

    3 жыл бұрын

    I totally agree.

  • @benjaminnielsen4288
    @benjaminnielsen42883 жыл бұрын

    That was a very appropriate ending. Thank You. What a tragic day that was.... God Bless

  • @PhlyDaily
    @PhlyDaily10 жыл бұрын

    nice thanks for the comment and thanks for the support

  • @DriverTheIntern

    @DriverTheIntern

    3 жыл бұрын

    Hey Phly, I love your content and i watch you every day on my other account.I know you know alot about planes so what was the plane next to voodoo and next to the ghost? 2:25 I think its a bearcat or a LA-5.

  • @JL-vx9ri

    @JL-vx9ri

    3 жыл бұрын

    yo wow this is old

  • @johnwkindig1613

    @johnwkindig1613

    3 жыл бұрын

    Guess we found out what Phly was doing 7 years ago...

  • @cpt.squiggly8004

    @cpt.squiggly8004

    3 жыл бұрын

    Damn, 7 years ago.

  • @Voodoo1650
    @Voodoo165011 жыл бұрын

    Well if you actually watch the video past 50 seconds you will see that the music was only a filler before the engines started.Thanks for checking the video out anyways.

  • @Vliegnet
    @Vliegnet7 жыл бұрын

    Great video. I really enjoyed it!

  • @Voodoo1650
    @Voodoo165012 жыл бұрын

    These are highly modified P-51's, plus a few other makes as well.

  • @christopherdoff-sotta4441

    @christopherdoff-sotta4441

    3 жыл бұрын

    Just out of curiosity how many g's are you pulling on that downward leg

  • @FiveCentsPlease
    @FiveCentsPlease11 жыл бұрын

    True if the NTSB had concluded that the modifications caused the crash but they didn't The accident happened because of worn original fiber lock spline nuts on the elevator trim tab hinge attachments, leading to a flutter condition and loss of the trim tab linkages and rapid loss of control. In short, it was old fiber lock nuts and there is now a service bulletin for all P-51 aircraft to inspect the lock nuts and replace with newer nylon lock spline nuts.

  • @DavidPT40
    @DavidPT409 жыл бұрын

    What's the song at the very end of this video with harmonica?

  • @Voodoo1650

    @Voodoo1650

    9 жыл бұрын

    That song is Western Winds by Hans Olson

  • @sgtgrash
    @sgtgrash12 жыл бұрын

    I noted that the wingtips of the Ghost were severely clipped, something that was performed on some models of the Spitfire during WWII to increase roll rate. Aerodynamically, could this have been a contributory factor for the Ghost going into a high speed stall? An incredible video Voodoo and so very sensitively produced. My sympathies go out to Jimmy's family, friends and to those families of the spectators who paid the ultimate admission fee to watch this amazing sport. God bless you all...

  • @DriverTheIntern

    @DriverTheIntern

    3 жыл бұрын

    It was to reduce drag i believe and very dangerous giving it less lift

  • @jrcadet4
    @jrcadet412 жыл бұрын

    Painful to watch, but everyone who knows or cares about Unlimited air-racing wants to know what happened. Thanks for posting this.

  • @PhlyDaily
    @PhlyDaily10 жыл бұрын

    Love that last line in your comment

  • @Predator-yc5up

    @Predator-yc5up

    5 жыл бұрын

    I seem to be the first one to have recognized you here.

  • @69burns94

    @69burns94

    3 жыл бұрын

    We need a P-51 tribute Phly.. I think you are just the man to do this

  • @DriverTheIntern

    @DriverTheIntern

    3 жыл бұрын

    Jeez you were a smaller KZread when you posted this, also a colab with Bo Time Gaming would help with veiws

  • @Voodoo1650
    @Voodoo165012 жыл бұрын

    @chimandude Hi chimandude, that would be Hans Olson and the song is "Western Winds" you can find his songs and CD's on Amazon. Glad you enjoyed the video

  • @rampking1
    @rampking112 жыл бұрын

    The Spirit of Jimmy Leeward, the lost and injured fans and the Galloping Ghost P-51 will be with us forever and so will Unlimited Air Racing at Reno. Calm wind and Blue skies forever to all who were lost .

  • @farmer6987
    @farmer698710 жыл бұрын

    he fuck with the airframe and made unapproved modifications. A real cowboy. To bad he killed people with his arrogance.

  • @FiveCentsPlease
    @FiveCentsPlease11 жыл бұрын

    The plane was modified with a "boil off" cooling system, with the radiator submerged in a water/alcohol mixture that's also used for the ADI system. You can see steam venting in some videos. One wing fuel tank was ADI fluid and the other wing tank was racing avgas.

  • @BE36pilot
    @BE36pilot12 жыл бұрын

    @CHUCKLOVES1969 An old friend, a former long time head of the Competition Committee said Jimmy was universally well thought of as an experienced unlimited racer and had been for the almost 30 years he had known him. The VP of the Unlimited Racing Class and head of the Safety Committee believes the cause of the crash was possibly due to The Galloping Ghost having a CG too close to the aft limit which resulted in pitch instability. They were using a tank in the aft tank position for coolant

  • @markjessurun1294
    @markjessurun12944 жыл бұрын

    THANK YOU JIMMY for your excellent performance, i didn't know U however HANS OLSEN made me CRY for You !! HAVE A NICE FLIGHT AND GOD BLESS U !!!

  • @jimstand

    @jimstand

    2 жыл бұрын

    Jimmy was a first class jerk. He lied about his age. He shouldn't have been flying. Unfortunately 10 people paid the price.

  • @markjessurun1294

    @markjessurun1294

    2 жыл бұрын

    @@jimstand aint we all Assholes, Sometimes?? Give the man the Benefit of the Doubt he tried he died that some more people died that's called Destiny !! Life is short !!

  • @jimstand

    @jimstand

    2 жыл бұрын

    @@markjessurun1294 You are beyond stupid. I have never killed anyone.

  • @737driver
    @737driver12 жыл бұрын

    For those who are interested, at 8:58 exact you can see the trim tab break from the elevator. God bless his soul and God bless you all. Cheers

  • @aliensandscience
    @aliensandscience3 жыл бұрын

    8:58 you can see the trim tab breaks off after the steep climb

  • @FiveCentsPlease
    @FiveCentsPlease10 жыл бұрын

    No, he passed out from G-forces when the plane lost control. The G-loading calculations, photo and video analysis of control inputs, as well as details of the control surface failure are all summarized in the NTSB reports.

  • @TacticalOni
    @TacticalOni12 жыл бұрын

    @dirac33 Little things break. Apparently its down to the trim tab. It's happened before and the pilot survived. unfortunately this time the scenario didn't play out that way. It doesn't matter whether or not it was outside it's envelope. The Galloping Ghost was professionally modified, and it was built to take the stresses of air racing. The aeros weren't trashed, most of these planes share the same attributes. It comes back to what I said before. little things break. RIP Jimmy

  • @flyingtigre1
    @flyingtigre112 жыл бұрын

    Ahh! You guys are my idol. Love the start ups and the end. So powerful and tragic at the same time. I think the memory should also be to the innocent victims. god bless. F-1 p.s. watch people copying Leewards nose dive from your clip.

  • @sheldonholy
    @sheldonholy12 жыл бұрын

    8:58 clearly depicts the elevator trim tab breaking and departing the aircraft. This could indeed be why the strong g-forces were present that prevented Mr. Leeward's head from raising into the canopy.

  • @StayUpStrack
    @StayUpStrack12 жыл бұрын

    So sad.. It's clear there's an awful lot going wrong at the same time and from the point roll right it seems Jimmy was working hard to bring things back under control. Thanks for posting. Much respect to Jimmy, all who lost their lives, AND all those that have been hurt in this terrible accident.

  • @raymondanderson751

    @raymondanderson751

    8 ай бұрын

    With the amount if g-force he experienced at the moment the airplane pitched up he was probably unconscious almost instantly when it pitched up and was probably unconscious through the whole accident, never even knew it happened.

  • @airspeedmike
    @airspeedmike12 жыл бұрын

    Very tastefully and respectfully done. A nice tribute to Jimmy as well. Cheers!

  • @08jag81
    @08jag8111 жыл бұрын

    and the WWII P-51 did actually have a slight amount of jet thrust, some variants used a new radiator design that exploited the "Meredith Effect", in which heated air exited the radiator at a higher speed and was ducted out the back of the lower air inlet scoop.

  • @Voodoo1650
    @Voodoo165012 жыл бұрын

    Hi MarceloSabat, That would be Hans Olson and the song is "Western Winds" you can find his songs and CD's on Amazon.

  • @jaegertiger384
    @jaegertiger384 Жыл бұрын

    If you look at the aircraft a LOT of the wings' surface area was removed - the flaps are virtually at the tips of the wings.. In conjunction with other modifications, I expect it created the "perfect storm". Thereby, leading to composite factors of failure. When trying to squeeze out maximum speed at the cost of control surfaces, then a bad outcome is much more likely to occur.

  • @ppk62fla
    @ppk62fla9 жыл бұрын

    Jimmy's race plane was subject to a severe wake vortex event and sadly when Jimmy corrected the movement of the Galloping Ghost it was so quick and violent that he passed out the NTSB assessment of the accident mentioned that wake vortex was perhaps one of the likely causes I noticed the flags and pennants were flying straight out meaning prevailing winds were quite strong which also added to the severity of the wake vortex event My Deepest Sympathy to those killed and injured and the families and friends affected by this tragic accident.

  • @FiveCentsPlease

    @FiveCentsPlease

    8 жыл бұрын

    +ppk62fla The NTSB report says that a wake vortex was inconclusive (Aircraft Performance Study, Page 19.) Using GPS data from Galloping Ghost and Voodoo, the NTSB performed two estimations of the wake from Voodoo, allowing for wind drift, and both estimations did not align with the flight path of Galloping Ghost. They did qualify those estimates that there could be variances in the GPS data from Voodoo. Both wind gust and mach buffet were ruled out as the initial causes of the loss of control. The initial failure of the trim tab control rods was the most likely scenario.

  • @d.j.fearlessiam8125

    @d.j.fearlessiam8125

    6 жыл бұрын

    ppk62fla perhaps is assuming...Even the Board can't put a finger to EXACTLY what happened... Racing Aircraft is Dangerous! If it would of been another plane... same thing,Loss of Life... Aircraft crash,We don't want them to...but they do. The one thing People are leaving out is the part of the report that said the course setup put spectators to close to the RACE...R.I.P. All involved

  • @g550doc
    @g550doc11 жыл бұрын

    No, all of these planes are running piston powered engines. Be them the V12 merlins of the p51's, or radials in the others, there are no turbines in these planes. PURE POWER

  • @Voodoo1650
    @Voodoo165012 жыл бұрын

    @clutchcrgo Thanks Clutch, very much appreciated!!! You're correct, I have been in contact with the NTSB and have given them all the footage I shot of the plane from this year.

  • @fjbutch
    @fjbutch11 жыл бұрын

    Right on that one. Forces on these aircraft must be enormous...

  • @FiveCentsPlease
    @FiveCentsPlease11 жыл бұрын

    The aircraft pitched up violently, not down. The trim tab failure was flutter from the loss of the control linkages.

  • @ricksclick
    @ricksclick12 жыл бұрын

    I looked at the photos at the gov. reference and couldn't see a missing piece of the elevator trim tab as many had commented on. But I did see that the tail wheel suddenly extended.

  • @FiveCentsPlease
    @FiveCentsPlease11 жыл бұрын

    With the exception of engine cores and a few castings, the Mustangs can be built from new structure parts that are being made to support the demand for parts for flying P-51s. Some of the other racer types have retired back to stock military condition because they are more valuable to the collector market as a historical original than as a modified racer.

  • @Voodoo1650
    @Voodoo165012 жыл бұрын

    @RFKFANTS67 here is the website for that particular SeaFury sawbonesair

  • @shanisonrichards5378
    @shanisonrichards537812 жыл бұрын

    my grampa introduced me to Jimmy when I was 7, almost surreal how fast shit goes bad

  • @ericv8319
    @ericv8319 Жыл бұрын

    If you didn't see it, watch the elevator trim tab depart the aircraft at minute 8:58 in the footage.

  • @Alantheleopard
    @Alantheleopard12 жыл бұрын

    I know that, talking on The Galloping Ghost´s crash, everything happened so quick that probably there was no time for anybody to react, but if these aircraft have radios to contact with their ground crews, I wonder whether investigators ever interviewed the ground crew and noticed anything strange in their conversation with their pilot (if there was time for any conversation at all). RIP Jimmy Leeward and all spectators on the ground who are not now among us... Poor them all indeed...

  • @Voodoo1650
    @Voodoo165012 жыл бұрын

    @GoPro1997 It's the silver P-51, race # 177.

  • @FiveCentsPlease
    @FiveCentsPlease11 жыл бұрын

    The AMA examiner cleared him to fly and the crash was not caused by the age of the pilot. Also, there are pilots older the 74 who fly.

  • @Voodoo1650
    @Voodoo165011 жыл бұрын

    Hi HHacker1959, that would be Hans Olson and the song is "Western Winds" you can find his songs and CD's on Amazon.

  • @mbrazile1
    @mbrazile19 жыл бұрын

    What a shame that the relic airplane was so recklessly looked after. And obliterated.

  • @crissignori7482

    @crissignori7482

    5 жыл бұрын

    Planes are lovely but the lost loved ones is another and far important matter I would say.

  • @Davide79
    @Davide7910 жыл бұрын

    RIP

  • @polaris92220
    @polaris9222011 жыл бұрын

    I believe that was one of the "trim tabs" on the left elevator. I saw it in slow mo too, hanging by one end for a while and then finally being ripped clean off. I don't think it would have turned out different with anyone else in the cockpit.

  • @jimstand

    @jimstand

    2 жыл бұрын

    No one else did the stupid things that Jimmy did.

  • @Voodoo1650
    @Voodoo165012 жыл бұрын

    AlanMartinNala Unfortunately in this particular case he was unconscious and slumped over from the initial high G pull up all the way to impact, so the radio would not have helped.

  • @pat36a
    @pat36a3 жыл бұрын

    A series of catastrophic events turning into a tragedy.

  • @mrfender5001
    @mrfender50013 жыл бұрын

    Where is the rest of the video?

  • @BBWanna12
    @BBWanna1211 жыл бұрын

    Thanx Voodoo. It was a terribly sad day for all of us who know and love these races. Never missed one in the 14 years we lived there and probably would have died that day had we still since that is where are box seats usually were. God Bless Jimmy and his family and no comments from you who know nothing about the Air Races. As with ANY other motor sport there is danger for the pilot/driver and the attandees. The back of every ticket has a disclaimer and ppl who go should be aware of dangers.

  • @4thgenpilot
    @4thgenpilot12 жыл бұрын

    A great video for someone like me who has to know why.

  • @Elementalism
    @Elementalism9 жыл бұрын

    Reading the report it is interesting how a trim tab can cause this kind of destruction. When I saw the video in real time the first thing that came to my mind was snap roll. Which was a fatal issue on the P-51 during World War II that caused catastrophic results to the horizontal stabilizer

  • @jackhammer5468

    @jackhammer5468

    9 жыл бұрын

    BS... the failures on the airframe came from modifications and poor maintenance.

  • @wesleyhill4922
    @wesleyhill49228 жыл бұрын

    My God, what a tragic ending; you don't have to be an experienced pilot to know that there must have been a malfunction in the control surfaces of that plane...it rolled, and that's not good....the result is heartbreaking!

  • @KutWrite
    @KutWrite5 жыл бұрын

    Clicking on the link in the description to the NTSB report gives an error: "No such page."

  • @Voodoo1650

    @Voodoo1650

    5 жыл бұрын

    Yeah, I just checked as well, they must've shut that page down recently.

  • @FiveCentsPlease

    @FiveCentsPlease

    5 жыл бұрын

    +KutWrite The full accident docket is still available in the NTSB database. dms.ntsb.gov/pubdms/search/hitlist.cfm?docketID=51746&CFID=2476155&CFTOKEN=7889ef31662e59cf-FADFDE46-F60F-51CE-3DE182D08C5F693E

  • @fkerpants
    @fkerpants4 жыл бұрын

    Not only did Jimmy Leeward lie about his age in order to continue flying, he relentlessly modified an antique aircraft, failed to maintain it properly, pushed it beyond its capabilities and killed ten people when he crashed it. Hell, he even said on video before the race that all his modifications to the Ghost hadn't been tested. I can't for the life of me understand why a person would retain respect for him. In the pantheon of aeronautical fuckups, he was worse than Bud Holland, and in the end his arrogance devastated numerous lives. Rest in peace, my ass.

  • @PabloGonzalez-hv3td

    @PabloGonzalez-hv3td

    3 жыл бұрын

    The amount of modifications and his age had nothing to do with the crash.

  • @nigelalderman9178

    @nigelalderman9178

    3 жыл бұрын

    @@PabloGonzalez-hv3td The modifications made the P51 over sensitive in pitch so when the trim failed it pitched up at 17g which would incapacitate any pilot. Lack or maintenance and reusing $1 parts did the rest.

  • @PabloGonzalez-hv3td

    @PabloGonzalez-hv3td

    3 жыл бұрын

    @@nigelalderman9178 The violent pitch up was caused by the sudden loss of trim force at 500+ mph not by any inherent "pitch sensitivity".

  • @Justin81James
    @Justin81James10 жыл бұрын

    Anyone notice the left side trim tab break off in the last seconds of the video?

  • @svyt

    @svyt

    10 жыл бұрын

    Yep. And so did the NTSB. In fact, somewhat before you see it break off - just at the point where the accident sequence starts in the turn - the control linkage for that trim tab actually buckled from stress, putting the trim tab in the wrong position, which initiated the accident sequence.

  • @glipaz
    @glipaz12 жыл бұрын

    At 8:56 you can see the left horiz trim tab hanging off the back of the stabilizer. At 9:00, the trim is seen falling off the back of the airplane.

  • @guntherultraboltnovacrunch5248
    @guntherultraboltnovacrunch52487 жыл бұрын

    Lost some fans too, and according to the NTSB made numerous changes to the air frame without reporting and misrepresenting his age. 11 dead. Dozens injured.

  • @Wayfaring_Stranger1
    @Wayfaring_Stranger110 жыл бұрын

    The NTSB determined that the failure of the left elevator trim tab led to a 17G nose-up moment that incapacitated the pilot and led to the crash. However, from this video it looks to me like the aircraft was already in the uncontrolled pitch-up when the trim tab separated from the aircraft well into crash sequence.

  • @svyt

    @svyt

    10 жыл бұрын

    Read the NTSB report in detail. The failure of the trim tab was a separate event from its later separation from the aircraft. When it first failed, it was still attached to the aircraft, but its link mechanism buckled. That initial failure caused it to cease performing its aerodynamic function properly, which is what initiated the loss of control and the high-G pull up. Subsequent forces ultimately separated it from the aircraft, but the initial failure was not the same thing as the moment it can be seen separating and flying off.

  • @jesuschristneverlived6938
    @jesuschristneverlived69387 жыл бұрын

    Intro song?

  • @Voodoo1650

    @Voodoo1650

    7 жыл бұрын

    I can't remember off hand, I'm in the process of trying to find it on my PC.

  • @jesuschristneverlived6938

    @jesuschristneverlived6938

    7 жыл бұрын

    +Voodoo1650 It was a very good choice for a video with these old aeroplanes :)

  • @vanstry
    @vanstry12 жыл бұрын

    Thank you for putting up this video. I saw a similar roll of the ghost as he passed the home pylon on the previous lap. I seem to remember hearing some of the earlier racers say that the air was really rough on Friday with a lot of turbulence. I hope that they are able to figure out why this happened so it never happens again. We lost a lot of great people that day. I'll be back next year.

  • @fjbutch
    @fjbutch11 жыл бұрын

    I noticed his rear left Flap seemed to fall apart. You can see it in 'slow mo'

  • @FiveCentsPlease
    @FiveCentsPlease11 жыл бұрын

    The thing is, the historic aircraft have become so valuable (much like the rare collector cars at concours) that they will live on reconstructed with new-build components. Wreckage will pass on to a new owner who will rebuild it with the original serial number. A number of former Reno racers have returned to original condition because they are more valuable in stock form.

  • @chriscalderin6677
    @chriscalderin66773 жыл бұрын

    Great comments! I came here to encourage and a lot is here already

  • @phlodel
    @phlodel10 жыл бұрын

    it's a shame that millions were spent on radical modifications to make this aircraft fast but failure to perform routine maintenance caused so much destruction and death. Relatively common hardware failed. These parts should have been found and replaced while the aircraft was being prepared for racing.

  • @FatManDoubleZero

    @FatManDoubleZero

    10 жыл бұрын

    I agree with you 100 percent. Why would someone with a multi-million dollar investment "skimp" on some relatively inexpensive control surface fasteners?? It makes no sense to me. If he couldn't find original replacements with the same tensile strength, he should have had the fasteners "custom manufactured" by a specialty machine shop. It would have been money well spent. Concerning the modifications you mentioned, experts with the NTSB noted, that perhaps some of the modifications made did not in fact yield any real enhancement in speed or control performance and may have instead been detrimental. The NTSB also stated that none of the major modifications to this air craft were tested and certified as being "flight worthy" by the appropriate authorities. Another careless error in judgment by the owner.

  • @phlodel

    @phlodel

    10 жыл бұрын

    FatManDoubleZero I'd be really surprised if anything but standard lock nuts were required. Maybe the mechanic didn't take the time to acquire them and merely tightened them "until later". No excuse for that, especially on such a highly stressed machine.

  • @FiveCentsPlease

    @FiveCentsPlease

    10 жыл бұрын

    FatManDoubleZero The original spline lock nuts in the trim tab linkages were over 60 years old and had deteriorated fiber inserts. It's unfortunate that they were re-used in the rebuild. New spline nuts with nylon inserts are already available and a mandatory service to inspect and replace these components was issued for all flying P-51 aircraft in response to the accident. www.warbirds-eaa.org/news/2013%20-%2002_27%20-%20P-51%20Service%20Bulletin%20Issued.pdf

  • @MFGKirchdorf
    @MFGKirchdorf12 жыл бұрын

    R.I.P. Jimmy, Spectators and Ghost. Perfect photographer. You stopped capturing at the right moment !!! ★ ⓉⓊⓂⒷⓈ . ⓊⓅ ★

  • @Bajadreamers
    @Bajadreamers10 жыл бұрын

    Tastefully done - thank you. it's been some 2-1/2 years now. Most of us who were there, who love our races, know pretty much all the why's and hows now. done is done. You buy your ticket you take your chances - Which are still much safer than any given day on this nations highways! NASCAR, boat races, football games, movie theatres, etc. To live life fully is to accept that there are chances and dangers in life, although we don't feel our races are anywhere near the top of that list! We've seen enough of the goremonging videos - the ones the psychos drool over, this one was tasteful. And for those posting the crude and rude comments - they are just trying to get a rise out of folks, by shouting and touting their ignorance of the sport and of life in general, and are not worth the time it takes to reply to them.

  • @illGustavOlli
    @illGustavOlli11 жыл бұрын

    BELA HOMENAGEM.. TODOS PILOTOS BRASILEIROS SENTIMOS MUITO.

  • @OldManCassius
    @OldManCassius11 жыл бұрын

    How did Leeward keep that engine cool? I know he removed the lower scoop so where was he getting the air to cool the radiators?

  • @scottwins2

    @scottwins2

    4 жыл бұрын

    Its actually the intake for the oil cooler

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