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We Blew Up The most powerful GR Corolla in the World.......

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Пікірлер: 153

  • @christophergeldien9907
    @christophergeldien99074 ай бұрын

    Hate to be that guy.. but “why the engine blew up” is probably 36lbs of boost on stock internals. That thing was dope dude, sorry for your loss, time to build back stronger.

  • @remyche8768

    @remyche8768

    28 күн бұрын

    500hp isn't much for this engine. Maybe faulty part or build error. Plenty now in gr yaris with this power with the no upgraded pistons the corolla has.

  • @christophergeldien9907

    @christophergeldien9907

    28 күн бұрын

    @@remyche8768 it’s the 36lbs I’d worry about more than 500whp. That’s a lot for cast internals no matter what engine. But that’s pretty dope that lots are making 500whp.

  • @remyche8768

    @remyche8768

    28 күн бұрын

    @christophergeldien9907 your probably right, but back in Nov 10, 2021 Motive video did a gr yaris build that got 472hp on 36psi of boost, only had its valve springs upgraded, with the motor left unopened and the internals untouched. Helping achieve the feat is a new exhaust, bigger turbo and intercooler, and a fuel system capable of delivering buckets of E85 from a custom surge tank setup. Then I'm pretty sure once they put cams in they got over 500hp with lower boost. And that would of been the non upgraded stock internals. Think possibly some over tighten a bolt, set the engine down to hard and bumped it in a right spot. Iv owed my gr yaris since they first came out and never seen a g16e-gts blow up like this. Iv only seen the miss shifts

  • @simplejoysmedia
    @simplejoysmedia5 ай бұрын

    Lets just say, we appreciate y'all pushing the boundaries of this platform. It's a big ol bummer but I know y'all are gonna rebuild a beast. Side note, I don't think I've ever seen engine carnage quite like that 😂 Cheers y'all.

  • @jasondoulkeridis6202
    @jasondoulkeridis62025 ай бұрын

    Roll back 4 years to the original release data for the GR Yaris and you’ll find one of the special things about the G16E GTS was that it had no valve seats.

  • @NMTDevastator
    @NMTDevastator5 ай бұрын

    Dang that is tough. Thanks for pushing the limits though to keep progressing the platform!

  • @NemtecRacing

    @NemtecRacing

    5 ай бұрын

    Come back stronger than ever

  • @nicrandazzo758
    @nicrandazzo7585 ай бұрын

    Take it to the dealership. Should be covered under warranty. Its pretty close to stock 😅

  • @Speedcamel1222
    @Speedcamel12225 ай бұрын

    I hope you get the Corolla up and running quickly.. thanks for pushing the limits on it, it was amazing to watch

  • @NemtecRacing

    @NemtecRacing

    5 ай бұрын

    Working on a quick turnaround

  • @CG-yh6js
    @CG-yh6js5 ай бұрын

    Paying close attention to what works and what doesnt for my 2024 GRC. Thank you and keep modding it

  • @Dr.Bojie-Chan
    @Dr.Bojie-Chan5 ай бұрын

    While I have seen plenty of pistons shatter, that is the most complete shatter I have ever seen. I am surprised you guys did not explore the bolt you found in the girdle and the balance shaft weight. (unless the bolt was put there during disassembly). This is absolutely a shot in the dark but if the balance weight came off and struck the crank/rod, it may have created enough resonance to blow the piston up.

  • @himmihyme2665

    @himmihyme2665

    5 ай бұрын

    the bolt looked untouched and the mounting surface on the weight seemed in tact. i would have questioned that a bit more too i think.

  • @FeedYourGreed
    @FeedYourGreed5 ай бұрын

    I’m really enjoying following this GR Corolla build, huge bummer that this happened. Really appreciate some of the technical analysis you and the team provide. Hope it comes back better than ever after you sort how you want to move forward with it!

  • @andrewmerrick601
    @andrewmerrick6015 ай бұрын

    Dang man, sad to hear but awesome to witness and learn from. Ya'll are awesome. Really hoping you guys get to hit the track this year! Either way, I'm here for the state of the art motion picture, nothing is more entertaining than learning about my own car lol

  • @mpgcamo
    @mpgcamo5 ай бұрын

    I think you guys need uprated Valve Locks and Rocker Retainers to help keep the valves captive. Lamspeed keep these in stock. I would also recommend the Oil Pan Baffles help to maintain oil pressure under high loads and lateral and downhill heavy braking Gs. 5w30 or even 5w40 should be recommended on these GR Yaris and GR Corollas because honestly apart from fuel economy 0w20 just can't adequately protect the engine under heavy load.

  • @TheAnonomusGamers

    @TheAnonomusGamers

    5 ай бұрын

    Definitely think it dropped a valve

  • @NemtecRacing

    @NemtecRacing

    5 ай бұрын

    Definitely gonna go all out for oil mods in the new motor for sure

  • @NemtecRacing

    @NemtecRacing

    5 ай бұрын

    I agree. After looking at it for a few days and looking at the ecu logs it seems to be the only reasonable conclusion

  • @GRSuperSonicRed

    @GRSuperSonicRed

    5 ай бұрын

    Honestly I thought they put those valve locks for the rockers. 😢😢😢This is sad. That was my first mod.

  • @chitasao

    @chitasao

    5 ай бұрын

    Came into the comments just to see if anyone else thought it might have been the loose rockers/lack of retainers that I saw in the Denstoj video a few months back: kzread.info/dash/bejne/iGh9prt7nJiykag.html

  • @MangoGRC
    @MangoGRC5 ай бұрын

    damn that's rough! poor valvetrain, but thanks for documenting these things to raise awareness on the possible limitations of our cars. rocky road to the most badass GRC!

  • @NemtecRacing

    @NemtecRacing

    5 ай бұрын

    Yeah looks like you need to be very very sure about who builds your head and definitely don’t skip out on better parts!

  • @Electronica27
    @Electronica275 ай бұрын

    11:14 my best guess would definitely be rocker/valve related. Very common on both gr86 and GRY. These cars aren't built to be bouncing off redline. I don't plan on hitting redline until I get that rocker retainer kit installed.

  • @GRCorollas
    @GRCorollas5 ай бұрын

    I want to see the GR at the time attack! Hopefully you guys find the best way out possible and thank you for pushing the limits 💪🏼 learning a lot of the G16 with you guys! Keep it up

  • @JK-tu1xx
    @JK-tu1xx5 ай бұрын

    I'm going to go out on a limb and say that this was pre-detonation combined with previous heat cycle damage to the head and longer duration camshaft timing. The combination of factors is likely the culprit, it makes the most sense when considering the alternative possibilities. You can't really point a finger at one issue being the reason this happened.

  • @mengx94

    @mengx94

    5 ай бұрын

    Didn't change the break in oil at 621 miles as stated in manuel

  • @Haloruler64

    @Haloruler64

    5 ай бұрын

    @@mengx94 The manual doesn't state that you need to change the oil at 621 miles. It only states that the break-in process is 621 miles and not to beat on it. No oil change recommended, though I did mine anyway.

  • @DavTune

    @DavTune

    5 ай бұрын

    @@Haloruler64 621 miles lol we were doomed early on in that case

  • @Haloruler64

    @Haloruler64

    5 ай бұрын

    @@DavTune Bro the Porsche 718 demands 2000 miles of break-in! TWO THOUSAND! I dunno how they do it.

  • @timbattle3415
    @timbattle34155 ай бұрын

    Great opportunity for some future footage. I'm looking forward to it.

  • @NemtecRacing

    @NemtecRacing

    5 ай бұрын

    We’ve got plans already in motion so it should t be too long!

  • @Gr4yota
    @Gr4yota5 ай бұрын

    Im going to be praying for team nemtec after seeing this video

  • @hudsoncordero
    @hudsoncordero5 ай бұрын

    I guess it's a good thing that lamspeed sells blocks, heads and basically whatever else you'll need. I'm excited to see what 'all will do with the new motor.

  • @WhatupJesus69
    @WhatupJesus695 ай бұрын

    Sorry for your loss. Thoughts and prayers going out to the entire Nemtec family. 🙌 🙏 😢 🪦 #RIPG16

  • @cappinteddy3228
    @cappinteddy32285 ай бұрын

    Genuinely surprised the block survived as well as it did considering an entire piston grenaded itself down into the crankcase. Damn.

  • @FarrPete
    @FarrPete5 ай бұрын

    Piston #3 has left the chat... 💥

  • @ADT2525

    @ADT2525

    5 ай бұрын

    *Has left the planet!

  • @mengx94

    @mengx94

    5 ай бұрын

    Existence*

  • @RichValleyPicker
    @RichValleyPicker5 ай бұрын

    great video! I am committed to leaving mine stock(Core with LSD's),but I love these videos of guys pushing these things!

  • @timprice8877
    @timprice88775 ай бұрын

    I’m so happy I bought my Type R 😊 Making 450whp on a bone stock block for 2 years now without a single issue , keep those torque numbers low & she will last!

  • @remyche8768

    @remyche8768

    28 күн бұрын

    @timprice8877 iv beat type r with that much power in my stock gr yaris, because he couldn't get traction

  • @timprice8877

    @timprice8877

    12 күн бұрын

    @@remyche8768 Ugh 😩 The things I would do to have a Yaris GR shipped to the states! Would love to make FiestaST AWD with 2.0 ecoboost head, & 2.3 ecoboost block, That’s about the closest I’ll ever get here in the states 😂

  • @JamesDyer90
    @JamesDyer905 ай бұрын

    The valve seats being MIA is odd for sure, im not sure if any other cars have failed in a similar way.

  • @NemtecRacing

    @NemtecRacing

    5 ай бұрын

    seems like not having rocker retainers mixed with some iffy head work might have been the issue. But im just a guy trynna have fun lol not totally sure

  • @GhostlyVG
    @GhostlyVG5 ай бұрын

    Damn man, sorry to see this. Thanks for the documentation. Excited to see what's next.

  • @NemtecRacing

    @NemtecRacing

    5 ай бұрын

    Soon we will get your reactions lol

  • @TylersNeighborhoodGarage
    @TylersNeighborhoodGarageАй бұрын

    Here's an alternative that will save 30k...buy clean 1970 Olds Cutlass, build 550 NA horsepower Olds 455, install drag radials, run 12.0's all day and spend all the extra time and money having fun. Just a thought.

  • @robzilla609
    @robzilla6094 ай бұрын

    I think when you changed your oil you increased crankcase pressure and potential got blow by and compressed fuel and oil on the intake stroke. Than as piston 3 traveled to TDC it detonated your piston. That failure potentially put a mix of fuel and oil in the exhaust which cause the large flames. Thats my guess.

  • @antd2733

    @antd2733

    21 күн бұрын

    Does heaver weight oil increase pressure?

  • @L3GACYxiNsTiiNcT
    @L3GACYxiNsTiiNcT5 ай бұрын

    For next time use of these 4 oils 1.Amsoil Signature Series 2. LiquiMoly 3.Pennzoil ULTRA PLATINUM 4. HPL Oil Royal purple is junk for high performance engines Also did you originally obide by the 2,500Mile Engine Break in period? Everything in the engine needs to properly seat before beated on which couldve caused the valve failure

  • @DavTune

    @DavTune

    5 ай бұрын

    I'm not sure the car even has 2500 miles on it quite yet

  • @mengx94

    @mengx94

    5 ай бұрын

    All bandaids

  • @SethWild
    @SethWild5 ай бұрын

    Painful to watch, but you guys are killing it. Hopefully there's a little more unreleased footage after the sequential install?!

  • @cpftank09
    @cpftank095 ай бұрын

    Damn, this doing it for science thing gets expensive!! Great videos and I hope you get it going again to race it this year.

  • @NemtecRacing

    @NemtecRacing

    5 ай бұрын

    Thanks for the support!!

  • @PierreCox97
    @PierreCox973 ай бұрын

    The flame looked cool at first…then I realized that’s when it blew 😭

  • @Quickb3n
    @Quickb3n2 ай бұрын

    I've seen a number of these blocks blowing completely untuned and running stock boost. I can absolutely see these being a depreciation bomb and almost un-buyable second hand once they start hitting high mileage.

  • @richurro20

    @richurro20

    Ай бұрын

    Same. No wonder in the GR Corolla FB groups everyone seems to be selling theirs off and more and more are starting to go for MSRP at dealers.

  • @alberttsai3659
    @alberttsai36593 ай бұрын

    I love how you guys constantly break stuff purely for our entertainment and enjoyment!

  • @Lairex_Rai
    @Lairex_Rai5 ай бұрын

    That sucks, just now watch the video and damn the piston just Grenades in there. Didn't you have a anti lag tune at one point? But that's just crazy. I hope you find out what really happened. It's still a new platform and trial and error.

  • @Andyol14
    @Andyol145 ай бұрын

    Cmon man looking weldable for sure!

  • @NemtecRacing

    @NemtecRacing

    5 ай бұрын

    100%

  • @mengx94

    @mengx94

    5 ай бұрын

    Jb* go brrrr

  • @someidiot9343
    @someidiot93435 ай бұрын

    Billet block to match billet trans?

  • @NemtecRacing

    @NemtecRacing

    5 ай бұрын

    That would be sooo sick but idk if anyone makes it lol

  • @begbis
    @begbis3 ай бұрын

    Seems like Royal Purple HPS 5w-30 has way too much calcium additive and that doesn't help with LSPI.

  • @austinwolfe2373
    @austinwolfe23735 ай бұрын

    That is impressive! Absolutely kachowed that engine 😂💀

  • @Jeditilt
    @Jeditilt3 ай бұрын

    IDK Wtf happened, I'm not a car tech like you all. but this is interesting AF! Can't wait for the upcoming episodes!

  • @user-ft6nr2ho9g
    @user-ft6nr2ho9g5 ай бұрын

    Is it possible that cyl 3 ran lean? overheated and cracked the piston?

  • @GeraldPUR
    @GeraldPUR4 ай бұрын

    So you gona buy a new motor? That crack looks unfixable. 😮

  • @NemtecRacing

    @NemtecRacing

    4 ай бұрын

    yeah there will be a video on it next week

  • @Robiam85
    @Robiam855 ай бұрын

    Looks like balance shaft went since it was directly under cylinder 3. Is there a balance shaft delete for these?

  • @bash5552
    @bash55525 ай бұрын

    check the springs, prob not strong enough, valve float due to rpm/boost, piston smash valve closed, disrupt seat, seat turns when valve open, valve cant close, piston not forged, by by piston, tears

  • @mhk67091
    @mhk670915 ай бұрын

    Pre detention is my thinking .. the look of that piston being completely shredded. Time to order a new short block!

  • @jhowe67
    @jhowe675 ай бұрын

    I'd bet the valve snapped, and at the high RPM, just turned into a blender. If the piston failed first, the wrist pin would be deformed or broken. The Guys in Europ making 600 to the wheels in the yaris have all gone to Forged pistons and rods, But they are also changing the valves at that power level.

  • @PaintflowException
    @PaintflowException5 ай бұрын

    IIRC I dont think thr pistons are forged... Thats unfortunate...

  • @boiipauly
    @boiipauly5 ай бұрын

    This will be a good discussion to compare how this happened vs the gry in europe making 700whp without blowing the motor.

  • @ireallyreallyreallylikethisimg

    @ireallyreallyreallylikethisimg

    5 ай бұрын

    That's insane, I wonder how long it could be pushed to 500hp for 😮

  • @boiipauly

    @boiipauly

    5 ай бұрын

    @@ireallyreallyreallylikethisimg i want to tune my grc to push 340-350whp but after seeing this I want to wait to see the proper precaution mods to do first after nemtec figures out what went wrong

  • @user-ln5bs5jo9k

    @user-ln5bs5jo9k

    5 ай бұрын

    Its Australia, not Europe, and they ran 770whp with a shot of nitrous. They said it was stock bottom end and only changed cams and valve springs, and ofc huge turbo. A g35-something, they didnt specify. It didnt blow up even while making multiple live stream pulls. They said they're going to do some work with it and bring it to the drag strip soon, so really excited.

  • @boiipauly

    @boiipauly

    5 ай бұрын

    @@user-ln5bs5jo9k well Australia, my bad didn’t do my research. I’m just curious since its the same motor why nemtec had this issue and the gry didnt

  • @user-ln5bs5jo9k

    @user-ln5bs5jo9k

    5 ай бұрын

    @vhofdimer6378 yea, same. It's really strange, and in Bahrain from ekanooracing, their fully built yaris has 600awhp. Multiple g16 engines are running 450+ now, and not many have blown up. Before you modify your own grc, you should ask for advice from lamspeed racing as they have done the most research and sell the most useful parts for the g16e engine.

  • @copperkeyracing6167
    @copperkeyracing61675 ай бұрын

    This is terroble to hear. Completely doesn't seem like it was something you did wrong. Seems like the proper precautions and care were taken (correctly sized turbo with the factory pistons and rods). I've never heard of the seats dropping out. My initial thought was a misshift at one time fatigued a valve but didn't cause it to bend completely. Then, one day, the valve gave out from being a fatigued valve, aka very ever so slightly bent valve... but that would be an exhaust valve, not an intake valve, and that's not the case. And then we find out the seat dropped out, and that's not something that can be banged out and must be pushed from the back or pulled out... that's just unheard of. It's easy to just pass it off as a factory defect, and defects do happen, but that would be too easy and nearly impossible to be likely. This is just completely a mystery. Maybe the shop that ground them actually did something wrong. Maybe they heated them. Maybe they did actually remove them and replace them without your knowledge... I would say that is most likely the answer to the mystery. Next time, don't let anyone touch the head, and/or ask for a video of the work done on it. Regardless, good luck. Love your work, and always watching.

  • @ajpwr666
    @ajpwr6665 ай бұрын

    I started to think that's not a coincident. All the G16 engines that failed were all Cylinder 3. By judging the head, the piston did smashed into the combustion chamber, the remaining 2 valves were pushed through the seat. I watched another Japanese video, that happened the same way, the guy said the piston disintegrated due to the coating technology that was used on the piston. Honestly, I think the G16 stock cannot handle anything over 400whp.

  • @NemtecRacing

    @NemtecRacing

    5 ай бұрын

    I’d say 420ish is probably fine. Our final dyno numbers were like 458whp so drop it by almost 40hp you should be good. Our new sequential added so much strain because it was just constantly in boost….

  • @NemtecRacing

    @NemtecRacing

    5 ай бұрын

    Do you know what video from Japan you watched that would be interesting to see

  • @ajpwr666

    @ajpwr666

    5 ай бұрын

    @@NemtecRacing I dunno where my respond went lol, here you go again. kzread.info/dash/bejne/da2BlNyYhbHZoc4.html The guy mentioned something about the latest coating on the piston causing it not generating heat and also to dissipate heat.

  • @Nameless-ej7xd
    @Nameless-ej7xd5 ай бұрын

    Thanks for the post Eared a subscription

  • @NemtecRacing

    @NemtecRacing

    5 ай бұрын

    Thanks for the sub!

  • @januaryandon2
    @januaryandon25 ай бұрын

    holy RIP lil engine

  • @dogsterooni
    @dogsterooni5 ай бұрын

    the cost to rebuild an engine

  • @Mike_OMara
    @Mike_OMaraАй бұрын

    Guessing your IDC’s was above 95%?

  • @vallasjo8003
    @vallasjo80032 ай бұрын

    Wow!

  • @rs3tuber425
    @rs3tuber4255 ай бұрын

    Watch this video, it is from Savagegesse and they do a 1 year review of all the most common fails on the GR Corolla. One of the weakest points is the valve train, it fails on the top end and it takes down the rest of the engine. Another fail is the rear diff overheating, the engine overheating and the crank knock. Just watch it: kzread.info/dash/bejne/nICE1quyhZDRptI.html

  • @dogsterooni
    @dogsterooni5 ай бұрын

    oh no

  • @spencervalentine3823
    @spencervalentine38235 ай бұрын

    What does insurance do in this situation

  • @CorkSportZach
    @CorkSportZach5 ай бұрын

    Damn JOHN!!!!!!!!! :(

  • @NemtecRacing

    @NemtecRacing

    5 ай бұрын

    It’s happens lol…. Sequential was just too addicting

  • @2seep
    @2seep5 ай бұрын

    How much hp?

  • @NemtecRacing

    @NemtecRacing

    5 ай бұрын

    450whp

  • @Crazy8ts
    @Crazy8ts5 ай бұрын

    so the engine and trans blew?, $$$$$

  • @Gr4yota
    @Gr4yota5 ай бұрын

    Any way to check the tune?

  • @NemtecRacing

    @NemtecRacing

    5 ай бұрын

    So on the ecu logs I made the 3rd to 4th shift and 2 seconds after the piston exploded…. We’ve talked to 2 different tuning shops around the world and compared notes and didn’t seem like ours was too aggressive in terms of timing etc we actually had a pretty conservative setup…. I think the head had a malfunction

  • @thatGRprick
    @thatGRprick5 ай бұрын

    Well damn 😢

  • @NemtecRacing

    @NemtecRacing

    5 ай бұрын

    It happens

  • @NigelsModellingBench
    @NigelsModellingBench5 ай бұрын

    This is crap.. sooo sorry guys. Didnt you say, when you had the head job that they fitted new seats? I wonder if they popped which is the sole cause of this issue?

  • @Faces98A
    @Faces98A5 ай бұрын

    Maybe a rocker slipped out??

  • @josemeza5086
    @josemeza50865 ай бұрын

    😥😥😥 my heart broke 😢sorry guys..that what happened

  • @mark_845
    @mark_8455 ай бұрын

    How much power did it have before it blew up

  • @NemtecRacing

    @NemtecRacing

    5 ай бұрын

    450whp

  • @seawarZz
    @seawarZz4 ай бұрын

    is piston alive ? :D

  • @man-e4g637
    @man-e4g6375 ай бұрын

    Detonation

  • @300zxdriver
    @300zxdriver5 ай бұрын

    Are you going to buy a complete engine?

  • @NemtecRacing

    @NemtecRacing

    5 ай бұрын

    No

  • @300zxdriver

    @300zxdriver

    5 ай бұрын

    @@NemtecRacing Can you buy a block?

  • @mengx94

    @mengx94

    5 ай бұрын

    Yea from moms ce. Or swap and start over. Mom gets an overbuilt engine for dd at tame levels 😆

  • @raymondfrank9202
    @raymondfrank92025 ай бұрын

    good one

  • @wossbros1
    @wossbros15 ай бұрын

    Good thing you got money apparently

  • @jeffreymitchell968
    @jeffreymitchell9683 ай бұрын

    Clearly it got very lean and melted a 1/3 of your motor. I would scrap it and buy a new engine there is no saving that engine. Check your logs I’m sure that cylinder was starved of fuel

  • @yoltsbp
    @yoltsbp5 ай бұрын

    Ooooofff honestly glad I bought a new wrx. These motors holding 660w stock 💪

  • @NemtecRacing

    @NemtecRacing

    5 ай бұрын

    Well power ain’t everything…. But I get your point

  • @Dobermann.Kennel
    @Dobermann.Kennel4 ай бұрын

    are you guys canadian?

  • @NemtecRacing

    @NemtecRacing

    4 ай бұрын

    No USA

  • @jeffreymitchell968
    @jeffreymitchell9683 ай бұрын

    Make sure you beef up the fuel system it’s the heart of the car. It’s obvious it was starved for fuel. Good luck with your build. I’ve seen a lot of people with damaged engines but your application is one of the worst failures I’ve ever seen.

  • @leolldankology
    @leolldankology5 ай бұрын

    JB Weld

  • @braxtonwebster8421
    @braxtonwebster84215 ай бұрын

    Warranty time

  • @DannySarbs

    @DannySarbs

    5 ай бұрын

    Yeah sure lol

  • @mengx94

    @mengx94

    5 ай бұрын

    But this is normal driving conditions?? Ryan tuerck drives it like this all the time 🤔😂

  • @BoostedRex
    @BoostedRex5 ай бұрын

    Sale Sale Sale!!!

  • @johnshoemaker6684
    @johnshoemaker66845 ай бұрын

    😢

  • @NemtecRacing

    @NemtecRacing

    5 ай бұрын

    It happens lol. We will be back

  • @khrizangel02001
    @khrizangel020014 ай бұрын

    Should’ve went 0w40, the 5w as a start viscosity. Can be the culprit

  • @Joel-um2oi
    @Joel-um2oi5 ай бұрын

    If it wasn’t valve float imma call it bad tune

  • @Alexi0
    @Alexi05 ай бұрын

    NOOOOOO

  • @HenHavenEggs
    @HenHavenEggs5 ай бұрын

    Yikes. So much for me telling my friends my cars block is bulletproof. Thr irony as I changed my profile photo tonight before watching this. Oops.... Ufo video tike rest of night.

  • @HenHavenEggs

    @HenHavenEggs

    5 ай бұрын

    Ill hang on hopes of hypereutectic piston failure. Kieth Black would be ashamed circa 1990.

  • @michaelfarrow25
    @michaelfarrow255 ай бұрын

    Rippp

  • @grcorollace
    @grcorollace5 ай бұрын

    just put it on rice

  • @carlosmoreno926
    @carlosmoreno9265 ай бұрын

    What's next?

  • @NemtecRacing

    @NemtecRacing

    5 ай бұрын

    New motor! More power lol

  • @lilripsta911
    @lilripsta9115 ай бұрын

    bad tune

  • @NemtecRacing

    @NemtecRacing

    5 ай бұрын

    Interesting opinion

  • @kickithard
    @kickithard5 ай бұрын

    Weak engine. This ain't no 2JZ.

  • @iJakku

    @iJakku

    5 ай бұрын

    If the 2jz was split in half into 3 cylinder. Its questionable that it'll be surviving this amount of power and boost either on stock block.